Syntax
Literate: Jurnal Ilmiah Indonesia p�ISSN: 2541-0849 e-ISSN: 2548-1398
Vol. 9, No.
7, Juli 2024
MANAGING
A MAJOR LUBE OIL LEAK ON A 150 MW STEAM TURBINE POWER PLANT
Msy
Cahaya Dinda Pamungkas1, Chelsi2
PT DSSP Power Sumsel, South
Sumatera, Indonesia1,2
Email: [email protected]1,
[email protected]2
The
reliable operation of steam turbines is paramount for the sustained performance
of electric power generation facilities. Any malfunction or breakdown in these
high-speed rotating machines can lead to significant operational disruptions,
causing energy production losses and jeopardizing safety. Lubricating oil leaks
represent a common challenge faced by power plants, impacting operational
efficiency, safety, and environmental sustainability. Despite extensive
research efforts to mitigate oil leakage, challenges persist due to the unique
design characteristics of power stations. This paper addresses the management
of a major lube oil leak in Unit No. 2 of the Sumsel-5 Power Plant in
Indonesia, focusing on innovative strategies for mitigation. The aim of this
research is to assess the effectiveness of various rectification measures in
reducing lubricating oil leaks in steam turbines. Methods employed include
detailed inspections, analysis of oil quality, and implementation of targeted
rectification strategies. The results demonstrate a significant reduction in
the oil leakage rate, from approximately 67-68 liters per day to around 1.5-2
liters per day, following the implementation of rectification measures. This
remarkable decrease of around 97.3% underscores the effectiveness of the
strategies in mitigating the oil leakage problem. The implications of this
study extend beyond operational efficiency to encompass safety and
environmental protection. By reducing the volume of oil lost to leakage, safety
hazards associated with fire accidents are mitigated, enhancing safety for
plant personnel and equipment integrity.
Introduction
The
steam turbine holds a critical position within electric power generation
facilities due to its pivotal role in converting thermal energy from boiler
steam into rotational motion. Unlike auxiliary equipment such as feed pumps or
fans, which offer redundancy to sustain operations at full or partial load, the
turbine's downtime directly translates to energy production losses (Chanda & Mukhopaddhyay, 2016; Idoniboyeobu &
Ojeleye, n.d.).
The
performance of high-speed rotating machinery, which is closely intertwined with
extensive and intricate industrial processes, is of utmost importance. Any
malfunction or breakdown of key components such as bearings, seals, and shafts
can result in either partial operational disruptions or complete shutdowns of
production systems (Ashraf et al., 2022; Portos et al., 2019).
It
is widely recognized that a catastrophic failure of a steam turbine, regardless
of its size, can have severe consequences, including causing serious injuries
or fatalities, leading to the complete loss of the machine, prolonged plant
shutdowns, and significant damage to the plant's reputation (Benammar & Tee, 2023). Despite extensive research and development
efforts aimed at preventing sudden rotor failures caused by bending, such
failures continue to occur in practice, resulting in substantial revenue losses
for plants. The costs associated with repairing turbines are exorbitant, and the
repair process often extends over lengthy periods. Therefore, ensuring the
reliability of rotor blades is paramount for the safe and successful operation
of steam turbines (Katinić & Kozak, 2018).
In
today's era of advanced aerodynamics, sophisticated rotordynamics capabilities,
and modern internal labyrinth seals made of polymer materials, it can be
incredibly frustrating for rotating equipment engineers to still grapple with
oil leaks. While these leaks must be addressed due to the genuine fire hazard
they pose and the risks associated with oil-coated surfaces, as well as the
time and resources expended on cleaning up and replenishing the wasted oil,
environmental considerations regarding oil containment and disposal also come
into play when dealing with machinery oil leaks (Rath et al., 2022).
Often, the root cause of these leaks is straightforward yet elusive, with
issues such as excessive clearance during seal installation, over-application
of sealing compounds on split lines, or blocked vents proving difficult to
identify once the machine is operational (Whalen & Krieser, 1998).
Lubricating
oil leakage in power plants poses significant challenges, impacting operational
efficiency, cost-effectiveness, safety, and environmental sustainability.
Various studies have highlighted the detrimental effects of oil leaks,
emphasizing the need for effective mitigation strategies. Sun et al. (2022) conducted research on a
hydropower plant in China, where the oil level in the tank decreased at an
average rate of 5�8 mm per day, with the water guide mechanism accumulating a
large amount of oil. Similarly, Deng et al. (2019) addressed the importance of re-designing cover plate
structures, achieving a notable reduction in oil mist leakage rates. These studies
underscore the complexity of the issue and the importance of innovative
solutions.
Lubricating
oil leaks can have multifaceted impacts, as noted by Wu (2017), who investigated the
activation of low oil level alarms due to leakage, leading to increased operational
costs and safety concerns. Liu and Deng (2010) observed
significant oil throwing on seals, causing rapid oil level drops in thrust
tanks and posing risks to personnel and equipment. Moreover, oil leakage can
have environmental consequences, as evidenced by research conducted by Jin and Bao (2017), where leaked lubricating
oil damaged water quality in a hydropower station in China.
In
response to these challenges, researchers have explored comprehensive measures
to address oil leakage problems. Wang et al. (2012) proposed the installation of comb labyrinth oil-retaining
tubes and oil baffle plates, while Cao (2010) increased
the height of oil-retaining tubes and installed oil-pressing vanes to mitigate
leakage in hydropower stations in China. However, due to the unique design
characteristics of power stations, there is no one-size-fits-all solution,
emphasizing the need for tailored approaches. In essence, while the challenge
of addressing oil waste in power plants remains complex and multifaceted, the
shift towards detailed characterization of oil flow fields offers a promising
avenue for developing customized, context-specific solutions (Sun et al., 2022). By
understanding the nuances of each power station's design and operation,
engineers can devise renovation plans that not only address current oil waste
issues but also anticipate and mitigate potential challenges in the future
Despite
extensive research on lubricating oil leaks in various types of power plants,
including hydropower facilities, limited attention has been given to steam
power plants, particularly those in Indonesia. The Sumsel-5 Power Plant in
South Sumatera, Indonesia, has been in operation for almost 8 years since its
commissioning in 2016. The Sumsel-5 power plant is facing persistent lube oil
leakage issues in Unit No. 2, necessitating effective management strategies. This
paper addresses this gap by discussing the management of a major lube oil leak
on Unit no. 2 of the Sumsel-5 Power Plant, with a focus on innovative
strategies for mitigating such issues.
In
addition, this research introduces a novel method for managing lubricating oil
leaks, particularly in steam turbines, by creating ventilation channels to
reduce leakage. The effectiveness of these improvements is evaluated based on
oil flow leak rates, cost savings, and ensuring that leakage rates are minimized
to manageable levels, allowing the power plant unit to operate at full load.
This study aims to contribute to the body of knowledge on lubricating oil leak
management in steam power plants, providing insights into effective mitigation
strategies for similar facilities worldwide.
Research Method
Chronology
of Failure and Fact-Finding
The
steam turbine is super high pressure, intermediate reheating, double casing,
double exhaust, sigle shaft and condensing type manufactured by Dongfang Steam
Turbine Co., LTD with a model N175-13.24/535/535. Sumsel-5 turbine has been in
operation since April 2016. The turbine structure can be seen on Fig. 1.
Figure 1. Turbine structure
The
turbine's rotation direction is clockwise when viewed from the turbine towards
the generator. This sophisticated turbine consists of a total of 31 stages,
divided across high-pressure (HP), intermediate-pressure (IP), and low-pressure
(LP) sections. The HP section includes one governing stage and eight pressure
stages, while the IP section comprises ten pressure stages. The LP section
consists of two sets of six pressure stages each. Furthermore, the turbine
incorporates a regenerative extraction system, featuring two HP heaters, one
deaerator, and four LP heaters. The main technical data of the steam turbine
are shown in Table 1.
Table I. Technical Data of The Turbine
No |
Name |
Data |
1 |
Rated
output |
175 MW |
2 |
Throttle
pressure (before MSV) |
13.24 MPa |
3 |
Throttle
temperature (before MSV) |
535 ℃ |
4 |
Reheat
pressure (before combined reheat valve) |
2.571 MPa |
5 |
Reheat
temperature (before combined reheat valve) |
535 ℃ |
6 |
Throttle
flow (TMCR) |
541200 kg/h |
7 |
Rated
exhaust pressure |
9.0 kPa |
8 |
Speed |
3000 r/min |
9 |
Final
feed water temperature |
249.7 ℃ |
10 |
Design
heat rate (TMCR) |
8430 Kj/kWh |
11 |
Maximum
output |
185.628 MW |
12 |
Maximum
throttle flow |
580000 kg/h |
The
whole shaft system is consisting of HIP rotor, LP rotor, generator rotor and
the connected main oil pump and exciter with total 5 bearings (3 bearings for
turbine and 2 for generator).
From
the inception of its operation in April 2016, the turbine functioned smoothly,
exhibiting consistently low shaft vibration levels across all bearings.
However, on January 26, 2018, the turbine encountered high bearing vibrations
on bearings No. 1 and 2 during startup. By 14:55, the rotor speed had reached
1100 rpm, escalating turbine bearing vibrations at 15:24 (1X: 161 μm, 2X:
168 μm). Subsequent speed reductions to 800 rpm (max Vibration 2X: 145 μm)
and then to 500 rpm (max Vibration 1Y: 212 μm) ensued, until the turbine
was manually halted at 400 rpm. The high vibration resulted from rubbing
between the rotating and stationary parts at the HIP turbine, notably from the
radial side, potentially involving components such as labyrinth packing and
diaphragm tip seals.
Possible
causes of rubbing at the HIP turbine were considered, including bearing
alignment, clearance inside the HIP TBN, and thermal expansion differences.
Despite analysis revealing no alarms or abnormalities in operational
parameters, lube oil leakage was discovered from bearing box No. 2 shortly
after successful synchronization on January 27, 2018. This incident led to a
fire, promptly extinguished through various corrective actions, including
turbine rotor cooling, dismantling and adjusting bearing No. 2 casing oil
deflectors, insulation work on the HIP line, and resetting lube oil and jacking
oil pressures before running the turning gear.
The
first overhaul conducted from September 22nd to October 27th, 2019. During this
period, vibration levels increased during startup on October 25th and 27th,
2019, resulting in the failure of both rolling attempts due to uncontrollable
increases in vibration. Subsequent inspection and treatment revealed rubbing at
both horizontal positions of the steam deflector plates and abnormalities in
the main oil pump, necessitating grinding, gap enlargement, and sharp-making of
the inner rings, as well as readjustment of bearing clearances.
The
turbine was restarted on October 27th, 2019, with the rolling process
eventually stabilizing at the rated speed of 3000 rpm, albeit displaying
characteristic forced vibration during speed rises, indicating the presence of
internal friction points within the casing. However, through the running-in
process, accompanied by casing warming and expansion, the internal friction
points gradually diminished, leading to decreased and stabilized vibrations. Fig.
2 shown the whole rolling process was as follows (speed-trend diagram, taking
1x as example).
Figure 2. Vibration trend
Despite the high vibration of all bearings remaining
within acceptable range values, the lube oil leak persisted from bearing box
No. 2. This underscored the importance of addressing the underlying issues
causing the leakage, even in the presence of acceptable vibration levels across
other bearings.
Rectification
Works
The
oil deflector plays a crucial role in driving the power generation turbine.
During the operation of lubrication equipment, oil leakage may occur. The oil
deflector serves as a device assembled on the bearing side and the exterior of
the rotor. It operates by creating negative pressure inside the oil tank, which
in turn draws external air into the interior of the oil deflector. This
mechanism effectively prevents foreign substances and fine dust particles from
the atmosphere from penetrating the system (Benammar & Tee, 2023).
After
the turbine overhaul process was carried out in 2019, wear was discovered on
the oil deflector labyrinth seals of bearing No. 1 and No. 2, induced oil
leaks. The solution involved replacing the oil deflector with a new spare part
and adjusting the radial clearance according to the design specifications, as
depicted in Figure 3.
Figure 3. Oil deflector replacement and clearance adjustment
�It was also found that the clearance of the
Front & Rear End Gland Sealing was outside the design range of 0.8-1.1 mm,
measuring instead between 1.8-2.0 mm. To address this issue, adjustments were
made to the clearance of the end gland sealing to align with the design
specifications. The occurrence of oil leak phenomenon is attributed to the
clearance of the gland sealing being outside the designated range. This
deviation may lead to steam leakage during operation, allowing for increased
levels of oil and steam condensate, ultimately resulting in overflow flow into
the bearing box.
During the Class A Turbine Overhaul conducted in
August - September 2023, the inspection of oil sealing wear and clearance was
repeated. It was discovered that there was wear on the blocking teeth
(labyrinth) of the oil seal, as depicted in Fig. 4. Additionally, the clearance
on the bottom oil sealing was found to be excessively large, measuring
approximately 0.3 mm, whereas the design requirement specifies a clearance of
0.05 mm - 0.10 mm. To address this issue, repairs were undertaken by
reinstalling the oil sealing in accordance with the specified clearance
requirements.
Figure 4. Wearing at blocking teeth (labyrinth)
of the oil seal
It was also discovered that the first row of rear
shaft steam sealing on the Intermediate Pressure Turbine side was covered with
oil sludge, as depicted in Fig. 5. Additionally, an inspection of the oil
return pipeline was conducted, revealing no defects or blockages in the
pipeline.
Figure 5. Oil sludge on
the intermediate pressure rear shaft steam sealing ring
The monitoring results of the oil leakage rate after
the overhaul are illustrated in Fig. 6. It is evident that there has been a
notable increase in the oil leakage rate. This escalation may have been caused
by improper gasket installation, leading to heightened vibration during startup
and exacerbating the oil leakage issue. In order to reduce the vibration to
within acceptable range values, adjustments were made by uninstalling the
gasket. Consequently, the vibration issues were resolved, but the oil leakage
rate from bearing box No. 2 increased, reaching 2800 ml/h at a full load of 174
MW.
Figure 6. Increment of oil leakage rate
�The decision to adjust the vacuum of the Main
Oil Tank to a more negative pressure of -900 Pa was a proactive measure aimed
at mitigating the risk of oil leakage from bearing No. 2 during continuous
operation. By increasing the vacuum, the pressure within the system is reduced,
potentially preventing the exacerbation of oil leaks. However, while this
adjustment helped maintain the severity of the oil leakage, it did not
effectively reduce the overall rate of oil leakage. This suggests that there
may be other contributing factors to the ongoing issue. One potential cause
identified is the possibility of the bearing box being completely filled with
oil, leading to trapped condensate pressure. This scenario can result in the
continuous decrease in the main oil tank level, requiring more frequent and
larger oil refills. Moreover, if the main oil tank level reaches the minimum
low alarm value, it could trigger a turbine trip, posing a significant
operational risk.
Figure
7. Piping & instrumentation diagram of the lube oil system
Figure
8. Installation of the venting line
To
address this issue, rectification measures were implemented during the
maintenance outage in February 2024. An additional venting line was installed,
connecting the oil level sight glass of bearing box No. 2 to the main oil tank
(Fig. 7 and Figure 8). This new venting line serves to release condensate
pressure within the bearing box, preventing overfilling and reducing the risk
of oil leaks. Furthermore, the improvement resulted in a reduction of the main
oil tank vacuum pressure from -900 Pa to -500 Pa. This adjustment was crucial
in controlling the oil level, alleviating the leakage rate, and preventing
overflow incidents.
The
installation of a fiber gasket at the side before the cover plate of the
sealing oil ring at bearing box No. 2 represents a targeted rectification
strategy aimed at reducing and managing the oil leakage rate. The position of
gasket installation is shown in Fig. 9. The decision to utilize a proper fiber
gasket with a thickness of 3 mm is based on its ability to provide a reliable
seal, effectively preventing oil leaks from occurring at this critical
juncture.
Figure
9. Cross sectional drawing of bearing ped between HP & IP turbine
The
addition of the fiber gasket serves to enhance the sealing effectiveness,
thereby reducing the likelihood of oil leakage and mitigating associated risks,
such as fire hazards and operational disruptions. Furthermore, by ensuring a
tight and secure seal, the fiber gasket helps maintain optimal operating
conditions within the bearing box, minimizing the ingress of external
contaminants and preserving the lubrication system's functionality.
Results and Discussion
The implementation of various rectification
measures to address the lube oil leakage issue from bearing box No. 2 has
yielded commendable results, leading to a significant reduction in the oil
leakage rate. As shown in Fig. 10, during full load operation, the average oil
leakage flow rate has decreased substantially from approximately 2826 ml/hr,
equivalent to 67-68 litres per day, to a mere 75 ml/hr, equivalent to 1.5-2
litres per day. This remarkable reduction represents a decrement of around
97.3%, indicating the effectiveness of the rectification efforts in mitigating
the oil leakage problem.
Figure
10. Decrement of oil leakage rate
Before
rectification, in order to maintain smooth operations and prevent the main oil
tank from reaching its low limit level alarm during major oil leakage
incidents, the plant incurred substantial costs. It necessitated the frequent
replenishment of lubrication oil, requiring the refill of 3 drums every 10
days, totaling approximately 9 drums per month and 108 drums annually.
Considering the use of Turbo Shell T-32 lubrication oil, priced at IDR
7,659,850 per drum, the cumulative costs amounted to IDR 827,263,800 per year.
However,
following the rectification measures and the subsequent reduction in the oil
leakage rate, there has been a significant decrease in the frequency of main
oil tank lube oil top-ups. Now, only 3 drums of oil are required for an entire
year, representing a considerable reduction in operational expenses. With the
decreased frequency of oil top-ups, the annual cost for lubrication oil now
amounts to IDR 22,979,550, resulting in substantial cost savings of
approximately IDR 804,284,250 per year.
The
rectification measures undertaken to address the lube oil leakage from the
turbine bearing box not only contributed to operational efficiency but also yielded
significant benefits from a safety and environmental perspective. Before
rectification, the presence of a major oil leak posed a serious fire hazard due
to the highly flammable nature of the lubricating oil and the proximity of the
leak to high-temperature components within the turbine. The potential for a
fire accident was a significant safety concern, posing risks to personnel
safety, equipment integrity, and overall plant operations.
Moreover,
the continuous oil leakage resulted in wastage of oil, leading to environmental
concerns. Oil spills can contaminate soil, water sources, and surrounding
ecosystems, posing risks to aquatic life and vegetation. Additionally, the
improper disposal of waste oil can further exacerbate environmental damage,
contributing to pollution and ecological degradation.
However,
with the implementation of rectification measures, the benefits in terms of
safety and environmental protection are substantial. By significantly reducing
the volume of oil lost to leakage, the risk of a fire accident has been
mitigated, enhancing safety for plant personnel and preventing potential damage
to equipment. Furthermore, the reduction in oil leakage minimizes environmental
impact by decreasing the amount of oil released into the surrounding environment.
After
many years of operation, lubrication systems can suddenly fail due to
degradation in lubricating oil quality. Therefore, regular monitoring is
essential. Although failures are rare, they can result in major damage to
turbine bearings and extended plant outages. Table 2 shows the analysis results
of the lubrication oil for turbine unit 2, which has remained normal for an
extended period. Wear metal analysis indicates no significant metal wear
contaminants, suggesting no substantial metal abrasion or wearing caused by
inappropriate operational conditions or lubrication. While the number of
particles counted does increase, it remains within normal limits, indicating
that the lubricant oil is still in good condition for circulation.
Table
2. Oil Analysis Monitoring Result
No |
Parameter |
Unit |
Method |
Result |
Limit |
|||||
Jan-23 |
Apr-23 |
Aug-23 |
Nov-23 |
Jan-24 |
Min |
Max |
||||
1 |
Kinematic Viscosity at 40�C |
cSt |
ASTM D445-21e2 |
31.46 |
31.56 |
32.03 |
32.07 |
31.95 |
25 |
38.4 |
2 |
Total Acid Number (TAN) |
Mg KO/g |
ASTM D474-22 |
0.03 |
0.03 |
0.05 |
0.05 |
0.05 |
|
0.45 |
3 |
Wear Metal |
ppm |
ASTM D5185-18 |
|
|
|
|
|
|
|
|
Iron (Fe) |
|
|
<1 |
<1 |
<1 |
<1 |
<1 |
|
30 |
|
Copper (Cu) |
|
|
<1 |
<1 |
<1 |
<1 |
<1 |
|
35 |
|
Aluminium (Al) |
|
|
<1 |
<1 |
<1 |
<1 |
<1 |
|
15 |
|
Chromium (Cr) |
|
|
<1 |
<1 |
<1 |
<1 |
<1 |
|
9 |
|
Nickel (Ni) |
|
|
<1 |
<1 |
<1 |
<1 |
<1 |
|
8 |
|
Tin (Sn) |
|
|
<1 |
<1 |
<1 |
<1 |
<1 |
|
10 |
|
Lead (Pb) |
|
|
<1 |
<1 |
<1 |
<1 |
<1 |
|
15 |
|
Sodium (Na) |
|
|
<1 |
<1 |
<1 |
<1 |
<1 |
|
60 |
|
Silicon (Si) |
|
|
2 |
1 |
1 |
1 |
1 |
|
15 |
4 |
Metal Additive |
Ppm |
ASTM D5185-18 |
|
|
|
|
|
|
|
|
Calcium (Ca) |
|
|
<1 |
<1 |
<1 |
<1 |
<1 |
|
|
|
Magnesium (Mg) |
|
|
<1 |
<1 |
<1 |
<1 |
<1 |
|
|
|
Zinc (Zn) |
|
|
5 |
5 |
4 |
5 |
5 |
|
|
5 |
Flash Point COC |
�C |
ASTM D92-18 |
228 |
223 |
226 |
232 |
223 |
|
|
6 |
Water Content by Karl Fisher |
ppm |
ASTM D6304-20 |
27 |
84 |
104 |
42 |
39 |
|
500 |
7 |
FTIR |
Abs/0.1 mm |
ASTM E2412-23 |
|
|
|
|
|
|
|
|
Oxidation |
|
|
<0.02 |
0.02 |
<0.02 |
<0.02 |
<0.02 |
|
0.3 |
8 |
Particle Counter |
|
ISO 4406:2021 and ISO 11500:2022 |
|
|
|
|
|
|
|
|
4 �m |
Counts/ml |
|
509 |
199 |
1468 |
484 |
1581 |
|
|
|
8 �m |
Counts/ml |
|
130 |
28 |
274 |
71 |
34 |
|
|
|
16 �m |
Counts/ml |
|
4 |
2 |
9 |
1 |
1 |
|
|
|
ISO Code 4406 |
- |
|
16/14/9 |
15/12/8 |
18/15/10 |
16/13/8 |
18/12/8 |
|
18/15 |
9 |
NAS Class |
|
NAS Class 1638 |
|
|
|
|
|
|
|
|
5-15 �m |
Counts/100 ml |
|
12280 |
2860 |
28140 |
6140 |
3600 |
|
|
|
15-25�m |
Counts/100 ml |
|
290 |
80 |
640 |
220 |
100 |
|
|
|
25-50 �m |
Counts/100 ml |
|
70 |
0 |
80 |
20 |
20 |
|
|
|
50-100 �m |
Counts/100 ml |
|
0 |
0 |
0 |
0 |
0 |
|
|
|
>100 �m |
Counts/100 ml |
|
0 |
0 |
0 |
0 |
0 |
|
|
|
NAS Class |
Counts/100 ml |
|
6 |
4 |
7 |
5 |
4 |
|
10 |
Conclusion
The
inspections conducted, along with subsequent investigations and rectification
efforts, were unable to completely eliminate the oil leak. Nevertheless, the
Sumsel-5 power plant succeeded in significantly reducing the volume of oil lost
to a manageable level. This allowed the machine to remain in operation,
effectively meeting the demand for electricity. The oil leakage rate was
notably diminished from approximately 67-68 liters per day to around 1.5-2
liters per day. Despite the ongoing oil leak, the steam turbine has continued
to operate smoothly, even under full load conditions, demonstrating its ability
to function with a manageable level of oil leakage.
Acknowledgment
The
authors gratefully acknowledge Mr. Lyu Yong Jun (CTO) and Mr. Chong Chee Shang
(IPP Plant Head) for their continuous effort in the characterization part of
the paper and their constant source of inspiration in writing it. The authors
are also grateful to all personnel at PT DSSP Power Sumsel for providing the
information necessary for the completion of this work.
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